Project: Doing it myself
#441
#442
#444
Drifting
#445
#446
Mine is a 2013. I pulled the original TB off with 4000 miles. It had the bronze blades.
#448
Nice! Where did you get those from?
#449
I ended up taking Unreal and Nino S' advice and cut my bumper support to allow more air to reach the intercooler and radiator. I have 3/16" or 1/4" steel plate at work. Im going to weld it into the open areas. It'll be allot stronger than before.
Then I put it on the ground and loaded it to get tuned.
Bye bye
Then I put it on the ground and loaded it to get tuned.
Bye bye
#451
No. Im going to let them take care of it. We've gone over every wire numerous times. They think it might be one bad wire or a bad ecm. They're going to go through the wiring and tune. Its in their hands now.
#453
Melting Slicks
did i miss or did you mention where the hood vets came from? i will do that for sure. ive seen the track spec ones but like your the ones you went with.
i went through every page of this and cant believe how much work has went into this GS. hope all is going well !!! keep it up man
i went through every page of this and cant believe how much work has went into this GS. hope all is going well !!! keep it up man
#454
did i miss or did you mention where the hood vets came from? i will do that for sure. ive seen the track spec ones but like your the ones you went with.
i went through every page of this and cant believe how much work has went into this GS. hope all is going well !!! keep it up man
i went through every page of this and cant believe how much work has went into this GS. hope all is going well !!! keep it up man
I thought I mentioned it but maybe it was in another thread. These aren't out yet. I don't know if they're going to make changes cause I had to modify mine. I'll have to get the company name when I get home. The company who makes them isn't the company who sells them.
#455
And for the update:
We found one of the wires for the throttle body was pinched inside the main harness and reran the wires. Reduced power mode was fixed. Got the car on the dyno. Fuel pumps 2 and 3 wouldn't turn on. Found out the catch can vacuum was robbing vacuum from the fuel pressure regulator off the vacuum block. We moved them away from each other and waiting for another dyno opening.
We found one of the wires for the throttle body was pinched inside the main harness and reran the wires. Reduced power mode was fixed. Got the car on the dyno. Fuel pumps 2 and 3 wouldn't turn on. Found out the catch can vacuum was robbing vacuum from the fuel pressure regulator off the vacuum block. We moved them away from each other and waiting for another dyno opening.
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Arctic Vette (11-19-2016)
#459
#460
oh ****! stick with it man, my car was a complete cluster kcuf when I first got it back and took me months of ironing out issues but it's been as reliable as a framing hammer now that I got it all figured out and it's tons of fun.