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416 ls3, built A6, Circle D 3600
GMPP ls3 cnc ported heads 230 int./242 exh. 112+3 LSA
Paxton 2200R
meth
flex fuel
It made 850 eating the belt, went 9.6 at 150 still eating the belt, in the heat, with a dirty air filter. I ended up finding out that the bearings in the supercharger had failed. The brass bearing cages came out of the supercharger as little nuggets that had clearly been in the gears attempting to stop the blowers rotation. The back cut A&A pulley was actually slicing chunks off the belt like a cheese grader. I have not been back to the dyno or track since fixing all the known issues.