1971 Journey





I was not after a wild cam, wanted it to idle and run smooth from low revs but have good torque low and mid.
The extra cubes will help as well :-)





I am trusting Terry to get it correct as I am no expert in this area.
He was comfortable I will be happy with the choice of components with a good low to mid torque band.
If I had better heads, like what Jethro is getting I think I could have had a more aggressive cam.
From the specs it looks like mine is between a Comp Cams 260h and 268h
There are as many opinions as there is web users on this issue and I welcome them all ... :-)
I read this from Chevy Performance and it seemed to make sense.
http://www.chevyhiperformance.com/te...m/viewall.html
If I look at that I am at the bottom of the degree for a 383 they recommend (214) but I dont have the better heads or diff ratio they are assuming for the build. My cam has more lift than the one they recommend for the 350 build though with stock heads.
So its done now so the seat of the pants meter will be the judge once I get it all back together.
Remember my aims were, reliable, good drive-ability and some improvements in torque and power (balanced more to torque than power at it wont live in high revs)
I only went to the 383 as the cost was minimal in the scheme of things, would have been happy with a rebuilt 350.





However I have mocked a few things up to check fit and alignment.

Last edited by CraigH; Apr 10, 2023 at 04:31 AM.





Put a final coat of paint on the block.
When it dries I will clean up the gasket areas.
Will also wet sand the sump as it has some runs and blemishes in it from when it was sprayed, mask it all up and give it another spray coat as well.



Last edited by CraigH; Apr 10, 2023 at 04:31 AM.





big thing is to get all the cam/lifter burnishing done instantly and not have a lifter not rotate due to lack of revs. have seen guys on net use old rocker covers with the top cut out so they can see all pushrods turning and if not grab pushrod and twist it around to start rotation.
good luck and keep revs up :o

That is something I have given a lot of thought into.
The cam comes with a break in lube additive that I will add to the Penrite Classic Lite oil that already has Z D D P in it.
The builder says start it up let it idle then drive it without letting it load or stress varying the revs.
Lots of web sits say get it towards 2000 revs and hold it there for 10-15 minutes.
A guy who works for me was an engine builder for years and tells me to follow what the builder has said as that's what he would have done. he believes the other methods (rev to 2000 etc) are all hangovers from a time past and don't really make sense any more.
To be honest i am not sure what to do !!!!





Some new bits and pieces.
Last edited by CraigH; Apr 10, 2023 at 04:31 AM.





So engine is fairly well ready to just fit all the accessories back on.
Pushed it outside and gave the engine bay a wash out first.

Last edited by CraigH; Apr 10, 2023 at 10:44 PM.





Starting point was around .025" endplay.
Hold distributor in vice.

Knock out the roll pin

Remove gear off bottom and add shims.

Measure how much play is present. I got it down to .013. Needed some different shims to get it better. Kit had 5 shims but only 2 sizes. .010 is meant to be about perfect.

The other thing to keep in mind (as reminded by Shipy59 way back in my thread) is the orientation of the bottom gear. The dimple needs to line up with the rotor pointer.
Why does it matter, well there is an uneven number of teeth on the gear so it places the orientation out by about 13 degrees. Makes it sit in the proper place and clear shielding etc etc, does not stop it from being timed properly. Mine was on wrong way when I took it out and I always had to fight the tach drive when I advanced it to its limit. Now with 13 degrees more movement it should be a bit easier.
Last edited by CraigH; Apr 10, 2023 at 04:31 AM.
The Best of Corvette for Corvette Enthusiasts





What tool to I need to remove the brass tack drive assembly to allow the shaft to come out ?






The gear drive mechanism.

Glad I did it as the grease well under the points plate was dry and crumbly. Originally I think they used something like a sawdust with oil in it. The bush has a hole to allow it to get on shaft.

All out and washed off.
Last edited by CraigH; Apr 10, 2023 at 04:30 AM.





i cant see that surface rust being left there too long either :-x
Thats whats in Lars's documents.
He suggests gauze soaked in oil rather than grease.
And yes that rust will have to go :-).
I found a washer on top of the top bearing that I think should not have been there. May have been to lower end float (wrong way).
If would result in rotor being higher than normal.
Have posted question NCRS to see if there was a washer there ever.





Top is fine but bottom had a little.
Cut through the lower bush on both sides with a hacksaw and tapped it out with an aluminum rod.
Placed new bush in a few mm to test and seems to be nice and snug with no movement.


Just need to go and get it pressed into place properly. or should i just buy a press and do it myself ? Could come in handy :-)
Last edited by CraigH; Apr 10, 2023 at 04:30 AM.






Last edited by CraigH; Apr 10, 2023 at 04:30 AM.





First fill the grease well with new grease and place plastic cap on.

Then fit felt ring.

Soak ring with oil.

Fit plate and retaining clip.

Grease and fit shaft, adding shims at base to get .010" end play. Fit tack drive cross shaft.

Fit advance weights and springs.


Fit rotor and cap.

Last edited by CraigH; Apr 10, 2023 at 04:30 AM.





The WT203-Z is on the money delivering the correct ohms resistance to correctly operate the C3 gauge.
Last edited by CraigH; Apr 10, 2023 at 04:30 AM.





I spun up the oil pump using a primer rod and battery drill to ensure I had oil flow to each rocker.




By using a 915mm length power steering belt you can get better access to the dip stick. The reproduction and originals are too short and foul with the alternator brackets.

Last edited by CraigH; Apr 10, 2023 at 04:29 AM.






So I needed to get some new brackets bent up.


The aim was not to need any mounting bolts so they needed to wrap around the top and bottom.
Using threaded plates behind the bracket to take the bolts.

Nice tight fit.




Last edited by CraigH; Apr 10, 2023 at 04:29 AM.





Radiator is aluminum painted black.





Made 2 seals for the lower fender to stop road dust getting in.
Reproductions did not fit well enough so cut larger ones.

Last edited by CraigH; Apr 10, 2023 at 10:46 PM.






