C5 Ignition Switch Repair
I have been having the service active handling bs for about 2 years now (we will see if that stops happening) and since 2 weeks ago I was having a strange problem at WOT in 2nd gear......at 3k rpms the car would cut out completely for a second or three and then be ok with no codes at all.

Last night I turned a sharp right in second and punched it and the car did the same but totally died
and every time I tried to restart it, it would fire then die ( about 30 times in a row).I then disconnected the bat for 20 sec and after that it fired right up.

This morning I pulled the ignition switch and cleaned and repaired it. After that I beat the car for 2 hours and it never happened again

Thanks for all the good info.
I bought the key cylinder here and you can also get the ignition switch.
Eventually the car started, before I had a chance to put a voltmeter on the Theft relay to see whether the issue is the ignition switch or the starter solenoid. If it no-starts again, that's the first check.
I'm not sure whether the engine started because I was moving the key around, or because I held it in the start position long enough to have solenoid finally kick in -- but either way, I would not have been nearly as far along as I am now without Bill's starting this thread
Last edited by mneblett; Nov 14, 2010 at 07:11 PM.
http://forums.corvetteforum.com/c5-s...ac-issues.html
Well atleast it gives me another option to investigate.
) and put things back together. Thought for sure I nailed it thanks again to Bill and the forum.BUT, after getting everything back together and trying to start her up, I got nothing!
long story short after taking a good look at things again, and pulling B2723, I noticed that the two white VATS wires got twisted during the work and they didn't look right....looked like the wires may be broken inside the plastic housing, so I took everything out knowing that you're dead without this great feature, cut the bad section out (which happen to be right by the ignition switch, a small ordeal in itself) soldered the wires and shrinkwrapped the finish product. - put it all back together and the 1st start was music to my ears....and 2nd, 3rd, 4th. etcThanks again to Bill and all forum members that chime in on their experiences and advice which keep our babies at home and not paying the ransom at any stealership.



WOW 
I know this is an old post but i'm a new guy and i'm still exploring !
What an amazing, well explained and detailed procedure !
I'll have to keep this one for future referrence !
Nice JOB Bill






THANKS Bill.

Here's what my old one looked like:






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My car was not shutting after long runs. Cleaned the ignition switch and the same contacts as above were much darker. Car shuts off everytime. Its a great feeling when what seems to be a big issue is so minor and free!
Thanks
Mark





Here are some steps that I believe will help make the repair work better and the switch handle a little more current!
Some additional guidance on the ignition switch repair.
Remember to re-arch the movable switch contacts so that they have better contact with the fixed contact point. Once there re-arched, you will need to use a hook (I used a bent paper clip) to ASSIST the arms over the FIXED contacts when your sliding them back into place!
Once the switch movable contact arms are in place, insert a piece of 600 grit wet and dry paper between the closed contacts and with a small pair of needle nose pliers or a pair of tweezers (I use a small pair of curved hemostats),, Move the sand paper between the contacts while applying some pressure on top of the movable arm. Switch to 1000 grit and polish the contacts. Clean the contacts with alcohol.
What your doing is making the CONTACT AREA of that single switch larger than it was. That will give the contact more current carrying ability and better contact. Do that to each of the FIVE switches....
REMEMBER!! Measure the resistance of EACH of the newly cleaned, re-arched, sanded and polished and cleaned contacts to make sure you have very very close to ZERO ohms resistance when the contacts are shut! If you have resistance, go back and CLEAN the contacts with alcohol again
Bill
Last edited by Bill Curlee; Sep 20, 2011 at 11:51 PM.
A question for you; When the contacts are cleaned up would you reccomend using a dab of dielectric grease on the contacts?
I've made a point of lubing all connectors with dielectric grease to help eliminate corrosion, but I'm not sure if it's a good idea on a switching contact or not. Advice?
A question for you; When the contacts are cleaned up would you reccomend using a dab of dielectric grease on the contacts?
I've made a point of lubing all connectors with dielectric grease to help eliminate corrosion, but I'm not sure if it's a good idea on a switching contact or not. Advice?
A question for you; When the contacts are cleaned up would you reccomend using a dab of dielectric grease on the contacts?
I've made a point of lubing all connectors with dielectric grease to help eliminate corrosion, but I'm not sure if it's a good idea on a switching contact or not. Advice?
Here's some reading for you: http://www.wisegeek.com/what-is-dielectric-grease.htm
Last edited by cdkcorvette7; Oct 11, 2011 at 02:08 PM.
Here's some reading for you: http://www.wisegeek.com/what-is-dielectric-grease.htm
"While the indicated use of dielectric grease calls for it to be used only on the non-metal parts of a connection, it has been shown to be effective at preventing corrosion when applied directly to the metal connectors as well. Care should be taken when using it in this way, because this application can, in some instances, cause the connection to stop working. A common reason for such a failure is that the grease has not been pushed entirely out of the way between the two points of contact."
This is why I've been using it inside connectors. Specifically, I put a little inside the female terminals so the male ends have to push through it when the connector is pushed together.
I've been doing this ever since I discovered that corroded fuel injector connector pins were causing weird problems at the drag strip... the car would run great out of the hole, then in 3rd gear it would lay down. Best time one night was 12.1 @ 112 MPH. 112 MPH in good air is pretty slow for a Z.
Researched, lubed all eight fuel injector connector's pins, pushed the connectors on and off a few times and have never had a problem since (traps instantly went up to 116 MPH and the car would pull cleanly through third and fourth). That was in 2004, the year I bought the car.
A sliding connection would not allow any significant amount of dielectric grease to keep a male/female pin/socket type of connection from happening... at least it seems to be working well for me.
BUT, knowing this (dielectric grease is an insulator) now I will definitely not apply dielectric grease to the contacts in the ignition switch. This type of contact seems as though it could definitely be affected by grease holding the contacts apart.
Thanks for the link!
"While the indicated use of dielectric grease calls for it to be used only on the non-metal parts of a connection, it has been shown to be effective at preventing corrosion when applied directly to the metal connectors as well. Care should be taken when using it in this way, because this application can, in some instances, cause the connection to stop working. A common reason for such a failure is that the grease has not been pushed entirely out of the way between the two points of contact."
This is why I've been using it inside connectors. Specifically, I put a little inside the female terminals so the male ends have to push through it when the connector is pushed together.
I've been doing this ever since I discovered that corroded fuel injector connector pins were causing weird problems at the drag strip... the car would run great out of the hole, then in 3rd gear it would lay down. Best time one night was 12.1 @ 112 MPH. 112 MPH in good air is pretty slow for a Z.
Researched, lubed all eight fuel injector connector's pins, pushed the connectors on and off a few times and have never had a problem since (traps instantly went up to 116 MPH and the car would pull cleanly through third and fourth). That was in 2004, the year I bought the car.
A sliding connection would not allow any significant amount of dielectric grease to keep a male/female pin/socket type of connection from happening... at least it seems to be working well for me.
BUT, knowing this (dielectric grease is an insulator) now I will definitely not apply dielectric grease to the contacts in the ignition switch. This type of contact seems as though it could definitely be affected by grease holding the contacts apart.
Thanks for the link!

Read the sentence immediately after the one you bolded. I'm not trying to be insulting or argumentative, but one of the main reasons why dielectric grease is such a great choice for things like spark plug boots is because it will not conduct electricity. That's not a the most ideal characteristic of a compound for use on electrical connectors. You want them to be made of the most conductive stuff plausible for the application.





I NEVER put Dielectric Grease in any electrical contact joint. Its a fantastic rubber lubricant and keeps moisture out of sealing gaskets, and you can apply it to electrical joints that have already been made like (
) battery terminal connectors and chassis ground terminals. A great anti corrosion agent are some of the marine products. Here is one that I have used with outstanding results and zero issues:

The ignition switch is not failing from contact corrosion. Their failing from poor contact and that causes contact heat and contact arcing. The arcing causes the contacts to carbon up and produce a high resistance contact point.
When you rebuild the switch, you can re-arch the contact arm to make better contact with the fixed contact point. You can also resurface the contacts using wet and dry paper to get more contact between the two contacts. That will enable the contacts to flow more current and produce less heat. I updated the post to include the procedure for sanding the contacts to provide more surface contact between the switches.
Bill















